Foreplay?
Every little thing is now done. All I need to do is cut the board off that fills the space from the door bottom where the concrete will eventually go and turn the two boards into one long one.
(The one side was made operable because that is the side my boat is on. Now the whole thing needs to be operable so I can drive in or out at will.)
Both the rear and tranny fluid I drained looked really good with hardly any "swarf".
It took f-o-r-e-v-e-r to fill the rear end back up! Thank God I had plenty of other things to do while it took its time s-l-o-w-l-y draining through that narrow tube. I just went with 4 pints as that was more than I got out. Someday I will buy another bottle and top it off.
Oh! It has a gasket! But the whole plate popped of perfectly! (hanging by the top bolt) The gasket looked really good, so I just cleaned everything up and screwed it back down. We'll see how that ends up working... (I'm thinking it will be fine.)
I reworked the wiring to the fuel gauge wahile I was piddling around. I also found out that the front cab mounts were never tightened down~ I left them loose so I could install all the front sheet metal.
Oddly, the fuel gauge now reads about a quarter of a tank. (Every time I turn the key on... This could be a good sign. I'll mark where the needle is when on tomorrow, then go get some more gas (cause I know I'll need it anyway) and see if the needle moved up or not.
Oh, BTW,
I DROVE MY TRUCK TODAY!!!
Backwards~ about 2 feet.
I couldn't believe how it spun the tires just putting it in reverse and *easing* it back! (My garage floor is currently gravel, misc. hardware and wood chips.)
Finally, I took my timing light and got the timing taken care of. It was just a tad off of where it was supposed to be.
Once that was done, I sat behind the wheel and gave it steadily more gas. Like running it up through the gears RPM kind of thing.
The higher the RPM, the more the missing.
This just won't do~ I am not taking it out on the street until I can have steady firing.
When I shut it down, I got out and checked the fuel filter up by the carb. Hardly a drop in it. It's kind of hard to run smooth if it's being starved of fuel.
WT???
Oh well, tomorrow is another day and this WILL get worked out!